The 355-Exposed? Covered Up? or Overlooked ???? | Page 5 | FerrariChat

The 355-Exposed? Covered Up? or Overlooked ????

Discussion in '348/355' started by bcwawright, Jun 5, 2007.

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  1. Artvonne

    Artvonne F1 Veteran

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    I dont know, but a lot of things on a car fail. The more performance you gain, the more difficult it becomes to try to keep it together. How hard were these cars driven, how well were they maintained, etc., those questions add into it too. I have cracked headers on my 308, its rather common on them too. But they arent making 109 HP per liter and running as hot either. This is why I am suggesting you expecting a lot. I dont think other than a Lambo, there are any other production cars with tube headers. And I dont know of any header manufacture that would warrantee a header longer than three years. The only other place you commonly see them is on aircraft, and all of those crack sooner or later too.
     
  2. bcwawright

    bcwawright F1 Veteran

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    Still waiting on valve guide analysis. Some points of interest that may be helpful.

    1. Exhaust valves are running about 50% hotter than intake,i.e.if intake is 800 deg then exhaust is around 1200 deg. Exhaust valve temps vary considerablly in comparison to the intake valve. It would appear from these numbers that if valve guide material is defective or not the correct design that the exhaust guides would fail long before intake guides.

    2. Approx. 75% of the heat dissipated from the valve comes from valve to valve seat contact, and approx. 25% of heat dissipation is thru the guide proper. If, the valve contact area is to small where it contacts tthe seat, or the stem length is too great, or if the valve guide to valve seat angle is off even just a little(this would also be the case if carbon deposits build up on valve seat or backside of valve), the valve begins to overheat. These are the things that cause burnt valves(this would also include excessive exhaust system back pressure,i.e. cloged cats or crushed pipess), and NOT CRACKED HEADERS. When valves are unable to dissipate the majority(75%) of the heat thru the seat then the valve guide gets alot of heat stress that it was not designed to take.

    3. Valve guide bore/valve stem clearance,valve stem height, and correct valve stem seals are absolutey CRITICAL.

    4. High quality Phos/Bronze valve guides that are properly installed should last approx. 40,000 miles.

    5. Fuel quality and additives DO make a difference. One thing I have noticed over the years is how gasoline formulas have been changed. When street engnes are designed they use materials that will withstand the corrosive effects associated with what was then the current fuel blends. I wonder just how big of an effect todays fuel has on older engine designs.

    6. When it comes to having your heads reconditioned DO NOT CUT CORNERS. This is not the time to be a penny pinching scrouge. Use the best, most highly skilled and equiped repair shop you can find.


    I will say that close is not good enough when it comes to doing a valve job......it HAS TO BE DEAD ON, especially when you have an engine like the 355 with high revs, radical cams/ignition timing. The temps that these engines operate at leave no room for error.

    Aftering reviewing many comments about Ferrari factory empoyees it is quite possible that human error in installing valve guides, seats, and valves is a major factor in the valve train failures being experienced. Also, after doing much research, guide/seat/valve production quality is still a major concern.......even Porsche is contending with poor quality guides in some of its' production runs.

    I find it very interesting that some of the cars that have had valve guide replacements are beginning to fail(wonder about the newer sintered steel ones). Also, I have even read that some of QV headers have failed. As for OEM headers, Vern has the right idea. Remove the heat shield and apply a thermal barrior coating(Jet-Hot is not acceptable for me), but even this is not the best way. IMO, the best way to go is to have a thermal barrior applied to the complete exhaust system up to the muffler, with a flow thru heat shield around the headers proper. The reason for coating the complete exhaust system is quite obvious....look how the pipes are routed near the trans oiling system, air intake system, and clutch cover........I would even go as far as recommending the clutch cover to have a thermal barrier applied along with a heat shield that incorporates an air scoop(similar to the part offered for the CH cars)......I even like the clutch cover that has the holes all the way around to help keep the clutch cool.

    As for OEM header material being crap(with the right design/coatings I can get mild steel headers to last)......it is not crap, it is just that the whole design is wrong. This is what Vern has already proven.....get rid of that mickey mouse lousy heat shield, coat the headers and they will last ALOT LONGER. Refurbishing the OEM with heavier guage metal(uncoated), and then putting that @#&* heat shield back on is not what I would do. If you think that heavy guage headers that take a fork lift to tote around is the cure then by all means go for it....while you're at it why don't you put a cast iron bumper on your high performance exotic so you don't have to worry about it cracking when you go over a speed bump. If a header is properly coated and shielded it weighs alot less, and it will even perform better. If you want your headers to LOOK stock OEM then you are going to have to live with these problems forever.

    It will be interesting to say ther least, how replaced valve guides, sintered steel guides,refurbished headers, and aftermarket headers hold up wth age and mileage.

    As for leak down and compression testing telling the whole story about valve guide condition???? Hmmmm....what do you think?
     
  3. bcwawright

    bcwawright F1 Veteran

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    In an effort to leave no stone unturned concerning valve guide issues I must include the cam. Side load thrusting inline with the cam lobe, and those forces that are perpendicular to the lobe may cause excessve wear to the valve guide. If the contact surface of "cam lob to tappet" is not square(not uniformly distributing the pressure) the valve stem tries to wobble......this effect is somewhat controlled by the springs/tappet assembly, but it is still an area I am looking at.

    Even more complex is the 5 valve design which has the intake valves in a radial array, which require one of the intake cam lobes(per cyl) to be at a different angle than the the other two. I am not sure of the jerk control built into the OEM cam, but if someone is more knowledgable about this I would like to know. As you can see, the angles involed with "cam to tappet", and then down inline to "valve guide to seat" are extremely critical.
    I know we are not building an F1 engine, but all of these things are important not only for better performance, but to make all that money you spent on reconditioning the heads last longer
     
  4. gothspeed

    gothspeed F1 World Champ

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    #104 gothspeed, Jul 20, 2007
    Last edited by a moderator: Sep 7, 2017
    Good info there bruce!! Though I think the 355 has similar lifters as the mondial/348 in that they have a 'tube' to slide in to insulate them from any lateral loads. Here is a pic I borrowed from lusso64's 30k mondial thread.
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  5. bcwawright

    bcwawright F1 Veteran

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    Yes, the 348 is a 2pc design with varying individual thickness tappets(shims)...355 is one piece design. Still looking at the cam though.e.g. angle of contact areas with tappet and tappet contact with valve.

    Please note, that I am forced to examine all of this in our quest to build a 10,500rpm 535hp engine. I have to not only look at VE, but even more so ME and TE. These are areas that I hope will unlock some major gains since the design/build incorporates stock OEM cams.

    BTW, does anyone have access to SLS equipment???????????????????
     
  6. gothspeed

    gothspeed F1 World Champ

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    Acronyms :confused:................ I need definitions :(
     
  7. bcwawright

    bcwawright F1 Veteran

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    Sorry about that.

    VE=volumetric efficency

    ME=mechanical eff.

    TE=thermal eff.

    SLS=selectve laser sintering
     
  8. UConn Husky

    UConn Husky F1 Rookie

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    Wait no longer! :) :) :)
     
  9. UConn Husky

    UConn Husky F1 Rookie

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    #109 UConn Husky, Jul 20, 2007
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    Here's the valve guide analysis, thanks to Dave for providing all these parts. As you can see from the picture, the guide color gives a good indication of the % Cu. At this point I'm not going to draw any conclusions from this, this is just another piece of the puzzle. From a chemistry standpoint it seemed like Ferrari took a step backward on the 355, until hardness testing revealed it had the highest hardness of the bunch (slightly). I haven't analyzed a new post '98 355 guide yet but will add that when we get one. After doing some reading and talking with automotive engineers one critical point was stressed - clearance between the guide and valve are absolutely critical and must be 'zero'. So one thought is that perhaps some 355's had the perfect 'zero' clearance and some didn't, resulting in a scattered failure rate. Then switching to a more durable guide made the assembly more robust to handle an ever so slightly wider range of clearances. (basically echoing what Bruce just stated above) That's all I'll theorize, and let the guys with infinitely more experience than me to comment!
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  10. No Doubt

    No Doubt Seven Time F1 World Champ

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    The 330 mid production to 330 late production makes a big change in zinc composition. If late 330's had fewer valve guide failures than mid production 330's then we need to look at Zinc?

    Interestingly, 355's have similar levels of Zinc to the mid production 330...while the 348 valve guides have levels of Zinc like the late production 330.

    Valve guide failures aren't an issue for the 348.

    What about mid production 330's?
     
  11. UConn Husky

    UConn Husky F1 Rookie

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    Yes much of this hinges on the actual failure rate, which we can only get anecdotal evidence of from the independents (unless we can get an insider to post actual data!!!) Interesting to me was the late 330 was identical to the 348 challenge, evidently they liked something about that one. And the late 330 and 348 challenge are bronze, while the others are really just high grade copper alloys (having more than 96% copper)
     
  12. davehelms

    davehelms F1 Rookie

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    Nice work Jay, thank you for your efforts with this.

    Knowing the composition and hardness is one facet of the equation. Add to this the load and pressures being exerted on the guides as yet another factor. The 355 uses 6MM stems where none of the others did. The 355 is running RPM's and valve acceleration rates exceeding the others, running FAR hotter than the others, and running a hydraulic lifter maintaining zero (or near to that) clearance. The environment the 355 stem is exposed to and the loading on the smaller stem far exceeds what the other models are seeing in average use.
    Brian Crall and I have long theorized that the initial assembly clearances varied car to car and was likely one factor in the high failure rate. With the small stem diameter, heat and RPM present in the 355 any "extra" clearance would cause a wear rate that would be exponential in nature. The 355 guides were simply not hard enough to handle the loads they were exposed to for very long.
    When the stem diameter dropped from 7mm to 6mm and the RPM and heat rose by (?)% the "hardness of the guide" should have followed in direct proportions. They did not.
    As the stem started walking around in the guide the seal was no longer able to control oil flow allowing a great deal of oil down the stem and into the combustion chamber. Oil mixed into the combustion process lowers the effective octane rating of the fuel being burned in that cylinder and thus causes another array of problems.
    Along comes the need for a "harder" guide and the steel replacements become available. Personally I have yet to see a failure of any of the steel guides. As Bruce wisely stated, this is an area that requires perfection in assembly and machining of both the guide fit and the seat to valve contact. I have seen many repair orders from both dealers and independent shops that state "Lap Valves" after guide installation. I assure you these will fail in short order and we will start to see burned valves as a result of the failure to properly machine both the seats and the valves after the guide replacement. We are talking about seconds of a degree in stem angle making all the difference in the world here. Even with the finest seat cutter machines it will require a very experienced machinist (that gives a damn) to hold to these tolerances. With that issue addressed will the same person be willing to accurately measure 40 valve stem heights before the machining process and accurately machine the stem ends back to the original assembled height. Remember, these have hydraulic lifters with a very narrow acceptable stem height range. Glass beading combustion chambers is a thing of the past (should have gone away when aluminum heads came about in my opinion) and few shops own a soda blaster to properly clean these heads. The 355 heads are riddled with very small oil flow ports to supply the hydraulic lifters that will not blow out clean with compressed air. All the threaded plugs need to be drilled and replugged after a complete cleaning if the heads get anywhere near a bead blaster.
    Did the machine shop pre-bore the guides to a very thin wall thickness, heat the heads in an oven to expand the aluminum and then gently press out the thin walled guide resulting in no gauling of the guide bore? Nope, I have had to machine a number of heads for oversized OD guides to date.
    There are so many factors involved in analyzing the failures of these components. I had to moth ball my $20K seat cutter and rely on my machinist who invested in a $130K cutter with digital readouts that is required to properly do this job. The seat angles and widths are so critical and so small it requires this type of investment in tooling and expertise.
    When we start to see a high failure rate of the valves or steel guides we will have to be careful about condemning the components and look closely at the expertise that went into the last machining process.
    Bruce said it best, DO NOT CUT CORNERS here!

    Dave
     
  13. No Doubt

    No Doubt Seven Time F1 World Champ

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    Dave, the critical tolerances/machining are amazing. That could easily explain the situation.

    On another note, if *materials* have any share of the blame, I'd think that we'd be able to figure that aspect out by examining the performance of mid production 330 valve guides versus late production 330 valve guides.

    Was there any noticeable difference in valve guide failures between mid to late 330's?
     
  14. davehelms

    davehelms F1 Rookie

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    No, none that I have noted.

    I think the steel guides would have been appropriate from the get go in terms of hardness considering the 6mm stem and the engine parameters. The reduction in supported surface area from 7MM to 6MM is quite drastic. With that said, I do share Bruce's concerns about the material selection but I have seen nothing to support these concerns.
    I felt just fine putting steel guides in my 1951 Ferguson tractor. To date all of the uses I have been exposed to where steel guides are present have a redline of under 6K.
    Material advances come about way faster than I can keep track of today. They may be just fine and I am judging them on my generic knowledge of the material from 15 yrs ago.

    It must be mentioned at this point that these are only my latest theories / thoughts and are not meant to be stated as fact. I do have a fair amount of recient tests and data that once reviewed seem to support these ideas.

    Dave
     
  15. No Doubt

    No Doubt Seven Time F1 World Champ

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    Thanks.

    Based on your comment above that the 330 mid production had no known difference in valve guide failures from the late production 330's, and considering the material composition of mid to late 330 valve guides compared to 348 valve guides and 355 valve guides, then we can conclude at this point that:

    MATERIAL COMPOSITION IS NOT AT FAULT in 355 valve guide failures.
     
  16. davehelms

    davehelms F1 Rookie

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    You must explain your logic and reasoning as it makes no sence to me.

    How did you factor in surface area (supported) and operating conditions and reach this conclution?

    I offer up thoughts I have based on as much data as I can obtain. Believe what you want, everyone will draw their own conclutions based on the debate but for goodness sake do not state things as fact.

    Unless you have additional data that is not being layed out, you can conclude NOTHING from this so far.

    Dave
     
  17. No Doubt

    No Doubt Seven Time F1 World Champ

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    My logic is this:
    1. the chemical composition as posted above for 330 mid production is strikingly similar to 355 valve guide composition, but the 330 mid production series (per your comments) had no unusual valve guide failure rates compared to late production 330 VG's.

    2. the chemical composition as posted above for 330 late production valve guides is strikingly similar to 348 Challenge valve guides which did not have unusual valve guide failure rates.

    CONCLUSION: material composition itself (not assembly, not tolerances, not design shape, not stem size, not heat/conditions/pressure, just the chemicals involved) is NOT to blame for the primary reason of 355 valve guide failures.
     
  18. bcwawright

    bcwawright F1 Veteran

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    Jay, sorry for the delay in responding to your analysis post. I do want to say a big thanks for the work. Because of your efforts it is now possible for the first time to actually see the factory receipe.
    I also want to thank Dave for contributing from his "Treasure Chest"(or should I say garbage pile), lol. Dave, I am just like you when it comes to saving bad or broken parts......who knows, one day all those things might be worth something, right??????

    I will be posting on the guides as soon as I can get my data and thoughts to agree....lol.

    Dave, do you have any info on the 355 guide that was tested,e.g. bore(each end, and the middle), mileage of car, int or exh(from color it appears to be int), and any noticeable wear of valve or seat, any carbon build-up on backside of valve?? I know you probably don't have any of this , but if you do I would like that info.
    It would of been great if we new the tolerances, guide bore, and valve stem dia. when this was new......anything that would makes this evaluation easier and as accurate as possible. But such is life, you can't always have everything "your way", like Burger King.
    TIA
     
  19. f355spider

    f355spider F1 World Champ
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    I'm not so sure that the cars are similar enough in design and operation to come to that conclusion. For example, we know that the 355 exhaust temps are much higher than the other cars; and max revs of 8500 are much higher than a 330. Would that not influence valve speed? Also, there may be a few other variables not being considered, such as valve material composition, that could influence the choice of valve guide material.
     
  20. No Doubt

    No Doubt Seven Time F1 World Champ

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    My point is more simple. The *materials* are not at fault based on the comparison to mid and late 330 valve guide materials, 330 valve guide failures, and 348 valve guide materials/failures.

    Could "design" be at fault? Yes. Possibly. Could assembly? Yes. Possibly.

    Could poor cam timing setting? Yes. Possibly.

    ...But we can rule out the materials per se based upon the data posted in this thread.
     
  21. davehelms

    davehelms F1 Rookie

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    Dave, do you have any info on the 355 guide that was tested,e.g. bore(each end, and the middle), mileage of car, int or exh(from color it appears to be int), and any noticeable wear of valve or seat, any carbon build-up on backside of valve?? I know you probably don't have any of this , but if you do I would like that info.


    They were bell mouthed on both ends like all of the failed guides. Std, bad guide carbon deposits. The guide to stem clearance on this engine was bad enough that the seal was unable to follow the stem. Std seat scuffing from the valve sliding into a seat position.
    I have my machinest bore the ID to less than 1MM wall thickness prior to removal so to save the bores in the head. I have had to machine dozens of OS guides to clean up "quickie" guide replacements and this has eliminated any gauling issues. I only remove 1 valve these days just for data collection as I have FAR too much time invested in this already. On this head the valves were dancing around ready to change holes.


    Jay, sorry for the delay in responding to your analysis post. I do want to say a big thanks for the work. Because of your efforts it is now possible for the first time to actually see the factory receipe.

    Boy, isnt that the truth! Without Jay's efforts we would be far behind the curve. So much of this effort is just to dot the i's which is something I need before making major changes to a Ferrari design. Accurate data like what Jay has provided doesnt come cheap! A big thanks again.


    My point is more simple. The *materials* are not at fault based on the comparison to mid and late 330 valve guide materials, 330 valve guide failures, and 348 valve guide materials/failures.

    Could "design" be at fault? Yes. Possibly. Could assembly? Yes. Possibly.

    Could poor cam timing setting? Yes. Possibly.

    ...But we can rule out the materials per se based upon the data posted in this thread.


    I have read it over and over and it still doesnt make sence to me.
    What works for one engine does not mean it will work for another of a completely different design. Material composition for a 330 running at low RPM, cold exhaust temps (compared to the 355), and large diameter valve stems is completely inadiquate for use with a 8500 RPM, 6MM valve stem.
    Cam timing has nothing to do with it, the guide doesnt care when the valve opens.
    Design may be a fault to some degree but if the geometry is correct all should be OK.
    Assembly is, as I stated before, still a thought but cant be verified. It is the one likely theory why some lasted longer than others that is left on the table after many others have been proven wrong.

    Material specs have to be properly matched to the operating conditions to obtain a proper cycle life. In this case they were not, but there are still two more tests that I am doing to prove my theory and verify my new design is up to the task. The key word is proof, anything less constitutes experimentation with a customers car which is not acceptable in my book. Hell, I bought a second 77 308 just so I had a base line (try explaining and justifing that to your wife!) on designs I am working on, the dyno only tells part of the story. There are a couple of problems with the 355 engine that have to be sorted and redesigned. I intend to own a 95 B soon and I want the long term reliabilty (read values) to be up to what I think they should be.

    No matter how you switch the words around, materials used to make the guides that are not matched to the task or operating conditions is still a material fault.

    Dave
     
  22. gothspeed

    gothspeed F1 World Champ

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    Wow!! What about a material that would better suit the operating environment of the 355? This would not be good if those 'other' potential causes you listed were to blame :( :(
     
  23. bcwawright

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    In this first of two posts, I would like to discusst the Sintered Iron guide.
    As a point of interest, sintering was a patented developement of one of my all time favorite motorcycle companies, BSA. They used this process for manufacturing the valve seats for the iron cylinder heads. This development was sold on company collapse to one of my least favorite car mfgs, Citreon, among others.

    Powder metal technology is absolutely awesome, as it allows the mixture of elements which could not be bonded together by any other manufacturing process. PM production is not just limited to ferrous, it also includes the non ferrous metals, i.e. sintered iron, sintered brass, and so forth.

    As with any alloy, it just doesn't appear out of nowhere, it requires many formulations with testing and analysis to create just the right receipe to meet the requirements of its' intended use.


    I do not know the complete receipe of the sintered iron guides Ferrari installed in 98-99 355s', but I do know three things which concern me.

    1. The sintered iron has an expansion rate which is 1/3 less than the aluminum alloy used in the cylinder heads. This brings into question its permanence, i.e. is it possible for the guide to become loose?? It is possible but I do not have a clue if that is something we will realize.

    2. This guide is inferior to the bronze in dissipating heat.

    3. The Ferrari PM iron guide is brittel. If you have valve failure the iron breaks off and does a doo-waa-diddy in the cylinder...ouch!! With copper alloy(bronze) this does not happen(atleast I've never seen it).

    Ferrari may have improved the receipe in the 360/430, but I do not know.
    You have to remember the iron guides for the 355 were spec'd in 1997 when PM guide receipes were playing catch-up to the high operating engine temps rerquired by EPA.

    It wasn't until 2005 that Hitachi Powdered Metals Company finally came up with the best of the best. This long legged beauty,Fe-Cu-Sn-C-P-MgSiO3-MnS...with free graphite, won the best new materials class by MFIP and EPMA!!!! This thing has better wear resistance than iron, easily machinable,has the same anti-seizure performance as brass on non coated valves, and darn good heat dissipation.

    Is it better than CuBe?.....NOPE!!! But its' as good as you can get in a sintered alloy..PERIOD. Are their other copper alloys that will work well? YES.....(1)manganese bronze, and (2) phosphorus bronze.

    So why did Ferrari switch from bronze to sinterred iron? After looking at the chemical analysis can you guess why?

    Side note here: I was talking with Bob Louthan(performance cylinder head specialist), who got a pair of heads off a late model 355, and guess what? One head had iron guides, and the other one had the bronze ones....WTF is going on n that Factory...lol
     
  24. BadHorsie

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    As far as keeping the heads cool has anyone looked at the engineering of the cooling system? Things like water jackets or water pump capacity? Are there any bottlenecks in the system? More efficient water flow is what I'm getting at here. I know from past experience with another car I was able to get a 30% increase in waterflow in the heads by machining out some flashing that was left over from the manufacturing process. Yes this created a 30% increase in flow something I think we would all be interested in if this was a possibility.
    You experts out there, are there any gains that can be made in that area?

    Steven
     
  25. bcwawright

    bcwawright F1 Veteran

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    We have touched on this subject(not in detail), in the thread by Gothspeed titled "355 spider idling problem is solved".
     

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