Spitfire "crash": pilot pulled wrong lever | Page 4 | FerrariChat

Spitfire "crash": pilot pulled wrong lever

Discussion in 'Aviation Chat' started by Nurburgringer, May 12, 2013.

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  1. Gatorrari

    Gatorrari F1 World Champ
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    Jim Pernikoff
    The Fw 190 I saw at Virginia Beach had a very bouncy landing, and someone said it always lands that way, a bit odd for a plane with wide landing gear. Maybe it had something to do with the shock absorbtion method.

    It's strange considering the disadvantages of a narrow landing gear just how many carrier aircraft had it: BF2C, SBC, F4F, Seafire, and the Bf 109 if the Graf Zeppelin had ever entered service.
     
  2. Bob Parks

    Bob Parks F1 Veteran
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    Just yesterday I looked at the FW190 in the Flying Heritage Collection and noticed that the oleo stroke is pretty short and of small diameter. However, the landings that I saw last summer were quite smooth so it could be the pilot or turf.
     
  3. James_Woods

    James_Woods F1 World Champ

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    Certainly it never had the bad ground-handling reputation of the BF-109. Strangely, Adolph Galland writes in his biography that he never much cared for the FW-190, and always preferred the Messerchmidt 109 (until he moved on to the ME-262).

    Everybody else says it was far superior to the 109.
     
  4. Bob Parks

    Bob Parks F1 Veteran
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    Galland. Another example of getting comfortable with what you started with and had success with. The ME109 did do some things better than the FW. It was lighter and smaller and a little bit better in a dog fight but it was limited and the FW190 could do a lot of things that the ME couldn't do. It was a great airplane.
     
  5. James_Woods

    James_Woods F1 World Champ

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    Conversely, Chuck Yeager (who flew all the captured types after the war) says in HIS book that the FW190 was the only one that was in the same class as the P-51 Mustang.

    Of the prop types, of course - he says the Me-262 was the equal of our later P-80.
     
  6. Bob Parks

    Bob Parks F1 Veteran
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    The specs for the F8F were to design the least airframe for the R-2800 that would produce the ultimate interceptor. That they did. I was able to see the F8F in April 1945 when the NACA labs were testing it and we were flabbergasted at the performance. We watched the NACA pilot do a max climb one day and it took off , went into what looked like an 80 deg. climb, and simply went out of sight. We couldn't see it but we could hear it as it kept going up. It made the P-51 H look like an old lady when they were flying together and dicing it out.
    We woke up one Sunday morning and there was this strange airplane sitting outside our barrack . There were no indications of what it was other then a dark blue paint job that indicated Navy. Later on we learned that it was a new Grumman and eventually found out that it was the F8F. Exciting and interesting days.
     
  7. snj5

    snj5 F1 World Champ

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    While I love V-12s as much as most, I happily contend that the Pratt and Whitney R-2800 is the finest internal combustion engine ever made.
     
  8. Bob Parks

    Bob Parks F1 Veteran
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    #83 Bob Parks, May 28, 2013
    Last edited: May 28, 2013
    I will always feel respect and admiration for the P&W engines but not up to the R4360. They did their best on this nightmare of mechanisms but it had reached the epitome of radial engines and suffered the consequences. Just too much going on with too much machinery to maintain reliability. The R2800 was and is a masterpiece. The R1830, R1340, and the R985 are gems. I feel that the only good Wrights were the J-4, the J-5, and the R1820. The original R3350 was nothing but a fancy boat anchor and the subsequent versions were somewhat better but no P&w. I got to thinking about the B-29 and its engines. Before I went into the service a B-29 crashed in a dry lake east of town due to engines on fire. When I was in basic training in Sheppard Field, Tex. I saw my first B-29 at about 10,000 ft. cruising overhead with number 1 on fire. When I was stationed at Langley Field one year later, I saw one coming in on final with an engine on fire. When I was walking out to the main gate at Drew Field after being discharged, there was one on short final with an engine on fire. Then in 1992 I got a flight and rode in the bomb aimer's position on FiFi when it was here for the 50th anniversary of the B-29 and I didn't have one worry about it and enjoyed the entire experience.
     
  9. Tcar

    Tcar F1 Rookie

    Bob, here's a pic of the Bearcat at NACA... is that you standing there by chance? (From Wiki).

    https://en.wikipedia.org/wiki/File:Grumman_XF8F-1_Bearcat_1945.jpg
     
  10. Tcar

    Tcar F1 Rookie

    I know those engines were tempermental... also heard that they had a huge problem with the props... many runaway props for seemingly no reason, which, of course did a number on a marginal engine.
     
  11. Bob Parks

    Bob Parks F1 Veteran
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    Geeze! That is the airplane but not me. B-24's in the background and in the distance you can see the dirigible hangar at the NE corner of the field. It was shot on the NACA ramp at a point just north of my barrack, Squadron A. That picture gives me a a real rush and I can tell you that I'll be thinking about that tonight after I go to bed. Thanks.
     
  12. I16

    I16 Formula 3

    Sep 15, 2008
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    Interesting report by the pilot! - very sorry if you have seen before, I did do a 'search' on FChat but could not find anything about the inadvertent flight.



    The flight in Taffy's own words
    This story is well known in Lightning circles but it is great to be able to hear the real facts 'from the horses mouth' as it were.

    Lightning XM135 Inadvertent Flight

    Some Background Considerations

    In attempting to write a more detailed personal account of my unfortunate flight in Lightning XM135 back in July 1966, I think I should add some of the reasoning and reason why I attempted the test in the first place. This might remove some of the erroneous facts, misapprehensions and misconceptions which I have seen in some accounts of the event.

    First I should explain that I was a qualified pilot, even although I was an R.A.F. Engineer Branch officer. I joined the R.A.F. as an apprentice in 1943, from where I gained a cadetship to university. At the university I read mechanical engineering and learnt to fly on Tiger Moths, with the University Air Squadron. On graduation, I was given the option to continue with an engineering career or to follow a General Duties (Flying) career. I chose the former path and the Air Ministry at that time, considered that there was merit in allowing me to qualify to 'wings' standard as a pilot, in the belief that an engineering officer with a pilot qualification, could more easily see the pilots point of view in aircraft maintenance matters. I too, thought this was a very good idea.

    I qualified on Harvards, but my early engineering duties only allowed me to keep in flying practice on Chipmunks. Whilst I was at Kinloss, I managed to get checked out on Oxfords and on occasions assisted a qualified test pilot, to air test twin engine Neptunes. My only jet aircraft experience was as a passenger in the second seat of a Javelin T3 and again in the 'rumble' seat of a Canberra. In my service, one of my postings took me to 33MU Lyneham where as the C.O of a civilian manned aircraft storage unit, I had Canberra, Meteor and Lightning types, which were gradually being prepared for despatch to various flying unit tasks. When the Meteor and Canberra types had been cleared, the powers that be, decided that the MU should close after the last Lightning's had been despatched. Up until the last Canberra, I had a qualified and current test pilot on my staff for those aircraft, but he was not a current Lightning pilot. When a Lightning needed test flying, I had to call for any available pilot with a current test pilot rating. Most times I would find one who could be spared within a 24 or 36 hour period. So much for my personal and R.A.F unit background.

    Lightning Mk 1A XM135

    XM 135 was being prepared for despatch to a Target Facilities Flight, but over a period of weeks, it had been giving no end of trouble. Each time it was being flight tested, the pilot found that on the initial few yards of a take off run, the inverter, supplying power to the primary flight instruments, would cut out and the stand by inverter would have to cut in, clearly an unsatisfactory state of affairs. Electricians were using every trick in their trade to establish the cause, each time thinking that they had removed, replaced and tightened every likely component. With nothing out of order, they would seek another test flight. It was a Boscombe Down pilot who next attempted to fly the aircraft, found the same problem persisting and refused to fly until a more positive explanation could be determined.

    Back to the drawing board, electricians decided to devise some tests which might isolate the fault and indicate roughly where and which component was at fault. They intended to ask the next test pilot to switch in and out parts of circuits, using trailing wires from the likely circuits to temporary switches in the cockpit and to do these electrical switchings before and after each few yards of a simulated take off run, when the fault was manifest. The temporary wires from internal circuitry required the cockpit canopy to be removed and in this state the aircraft was made ready for another air test. Being a pilot, it was easiest for me, as CO, to request the services of a qualified test pilot, from wherever I could find one, but for the next test on XM135, no pilot was available for at least another week. With my unit closing down, many civilians being made redundant, a timetable of clearance being upset with this 'rogue' aircraft, there was much tetchiness and irritation amongst my staff. The intended Boscombe Down pilot, knowing I was a pilot, suggested I might try the test myself. He suggested using an out of use runway (Runway36) as I would only be using 30 or 40 yards at a time. He suggested using a Trabant to communicate with Air Traffic Control and to get their clearance for each movement of the aircraft. However, there was one remaining minor problem. I had only sat in a Lightning cockpit once before and I had no idea how to start its two Rolls Royce Avon engines! The Foreman of engine trades gave me a 5 minute briefing on how to do this and XM135 was towed out to Runway 05 on 22July 1966 for my electrical tests.

    It was by way of extraordinary good fortune that my engine Foreman explained that, although I would not be needing reheat, that reheat needed the throttles to be pushed past a reheat 'gate' and one had to feel for the gate keys, behind the throttle, to unlock. My only other knowledge of the Lightning was what I could remember from pilot's notes. At each test flight by the qualified pilot, I would be in ATC with a copy pilot's notes, should he need any aircraft figures to be relayed to him. One or two figures stuck in my mind, namely that the undercarriage had a maximum speed before it should be retracted and I had an even vaguer figure of about 150 knots for a landing speed. Some extra knots would be required for each 1000 lbs. of unused fuel, but I did not need to bother with any such figures for the test, which I was to undertake.

    The Ground Test

    I was correctly strapped into the cockpit (seated on the in situ parachute and ejector seat) and after starting the engines and holding the aircraft static, on the brakes, I did the necessary preliminaries for the electrical checks in the cockpit, checking the notes I had scribbled on a notepad which lay on the coaming in front of me. All seemed ready for the first test and I indicated to the Trabant to obtain ATC clearance for use of the short 30 or 40 yards of runway. Holding the brakes I gradually opened the throttles to about 90%. My feeling at the time was the unexpected heavy vibration of Avon power held against the brakes. I did a quick check of the temporary electrical switches and circuitry lights, then released the brakes. That initial punch from the thrust was quite remarkable and I moved the expected 30 to 40 yards before I throttled back and applied the brakes. So far so good. I made some notes, altered some more switch positions, noted the on/off lights and prepared for the next test. This was done in a similar fashion and I was leaving the 'fault' diagnosis to my electrical staff who would have to interpret my notes. I needed to do one more test and ATC had noted that I had only used about 100 yards total, so they were quite happy to clear me for a similar short distance. ATC had also been holding up a fuel bowser and trailer with 3600 gallon of AVTAG for awaiting C130 aircraft refuelling, they decided to allow the bowser to cross the runway. On opening the throttles for that final test, I obviously pushed them too far, misinterpreting the thrust, because of the unexpected heavy vibration and they got locked into reheat. Yes, I did use some expletives but I had no time to think of getting out of reheat, because in front of me, the bowser and trailer had just crossed the runway, from right to left, so my thoughts were to make sure I was missing them by sufficient margin. No, I couldn't steer to clear them; reheat takes you in a straight path like a bullet out of a gun. The time between finding myself in reheat and just missing the bowser was less than half the time I have taken to write this sentence.

    Before my thoughts could again return to getting myself out of reheat, I was gathering speed and about to cross the main duty runway, where a Comet had just passed on its take off run. I then had no time to look for reheat gate keys, my eyes were on what next lay ahead. Two things, the end of the short runway 07 and just beyond was the small village of Bradenstoke which I just had to miss. There was no chance of stopping, non whatsoever. I had gained flying speed (that is what reheat is for, short sharp take offs) and I had no runway left. I did not need to heave it off the runway, the previous test pilot had trimmed it exactly for take off and only a slight backward touch on the stick and I was gathering height and speed. Then my thought was to get my speed back in case I should damage the undercarriage. Incidentally, I could not have raised the undercarriage; the ground servicing locks were in place for safety reasons. With only clear blue sky in front of me, I could then search and feel for those gate keys. Yes, I found them and thanked my lucky stars that my engine foreman had quite incidentally told me of their location and I was soon able to get the speed back to (I am guessing now) about 250knots. My next thoughts were to keep Lyneham airfield in sight and where had the Comet got to, the one I had missed a few seconds ago? Then I asked myself, should I eject and where and when? No, I could not; the safety pins were in the ejection seat and safe for servicing, not for flying. My only alternative then was to attempt a landing, but how does one interpolate or extrapolate Tiger Moth, Chipmunk, Harvard flying to a two engined, 11 ton, beast like the Lightning?

    After regaining my bearings, a little composure and simply by observation, making sure that the Comet had been warned away, I decided I should attempt a landing on the duty runway and direction. I was trying to combine all my limited flying experience into a few minutes of DIY flight 'training' on a Lightning. It wasn't easy, but I must admit that some of the elementary rudiments of my proper flying training and flight theory were coming in useful. I needed to get the feel of the aircraft, if I was to get it back on the ground. My first approach was ridiculous, I could tell that my speed, height, rate of descent, even alignment wasn't correct and my best plot was to go round again. This time making sure that my throttles would be well below reheat position. A second approach was no better, I had some aspects better, but as the duty runway 25 is on the lip of an escarpment, with a valley floor beyond, my rate of descent took me below runway height and I found myself adding power to get back to the right level. More power also meant more speed and I was trying to get to something like 150 knots for landing, but the uncoordinated attempt was becoming a mess so I abandoned it, took myself away on a very wide circuit of Lyneham and decided to land in the opposite direction. This I thought would give me more time to get the 'feel' right and if I made a mess of the landing, I would overrun the runway and just drop (crash) into the valley beyond. In that direction, with a messed up landing, I would have no fear of crashing into Lyneham village.

    The long final leg of this approach gave me the thinking time that I needed and I gradually got the feel that speed, alignment, rate of descent, height and approach angle were better. I plonked it down at about the right position off the runway threshold, but just forgot that I was in a nose wheel aircraft and emulated my best three wheelers in a Chipmunk or Harvard. The result was that I crunched the rubber block which encases the brake parachute cables. However, I had got down, but I then had to stop. I obviously knew the Lightning had a brake parachute, but where was the 'chute lever, button or knob? There, I found it marked Brake Chute and I pulled it and I could then look ahead and concentrate on keeping straight and somewhere near the centre line. I hung on to the brake lever, I wasn't slowing as much as I would like, so I just kept up my hand pressure on the brakes. I had about 100 yards of runway left when I stopped and even then, I didn't know that the brake parachute had dropped off as soon as it was deployed, because the cable had been severed as a result of my super tail wheel three pointer.

    Events Immediately after the Flight

    XM 135 was towed back to the hangar and I was taken to see the medical officer who gave me some pills to calm my nerves. I felt reasonably calm because I had almost killed myself on five occasions in that 12 minute flight, yet I had miraculously survived. What is more, I would see my wife and young family again. Two or three times in that same 12 minutes, I thought I would never ever see them again. My only priority was to save my own skin, I was not thinking about the non insured loss of a Lightning Mk 1A aircraft. The minor damage to the aircraft was repaired with a new set of brake shoes and a new rubber chute block. As a memento, I have kept that rubber block, one day it might be returned to XM135 at Duxford.

    The Fault

    Although the tests I did and the ensuing flight did not immediately provide a reason for the initial electrical fault, my electrical staff, with additional assistance from English Electric, Salmesbury eventually did. Apparently, in early versions of the Lightning, there was to be a ground test button fitted into the standby inverter circuit. It was never fitted to the Mk1A but the wires were left in the looms. It was one of these redundant wires which shorted on to the UHF radio as it moved on its trunnions when the aircraft nudged forward on take off. Who would have thought I should risk my life to find it, in the way I did?

    Events Subsequent to the Flight

    There was a subsequent Inquiry to find out what had happened and why and to make recommendations for it never to happen again. As I was the Commanding Officer of the Unit, I was responsible for my own as well as the service actions of all my staff. I was not acting against any orders in the Flight Order Book which I religiously kept up to date. But those orders did not cater for engineering officers doing investigative type checks on Lightning's. They were later amended. After the Unit Inquiry I had to go up in front of the Commander-in-Chief. That was when I thought my career would be placed in jeopardy. I even thought that my coveted 'wings' would be taken from me; I had no idea how the incident was being regarded by Command or indeed Air Ministry. But, as I stood in front of Air Marshal Sir Kenneth Porter, he read the proceedings, asked me if I agreed with his view that "With the limited flying experience that I had, the test would have been better left to an experienced and current Lightning test pilot." I agreed of course. He then told me to remove my hat, sit down and proceeded to tell me some of his unfortunate flying incidents in Mesopotamia in the Middle East. I was thankful that nothing more was to become of the incident and that I still had a job to do back at 33 Maintenance Unit, Lyneham.

    I coped with all the official communications regarding the incident, but what I was unprepared for was the release of the story to the public. I had had very little experience of working with the press, certainly none with radio, TV, national and world press. I had no training in how to deal with their quest for news. My Command Headquarters suggested I went away on leave before press releases were made by Air Ministry. This I did and took my family off camping to Jesola, in Italy. Imagine my complete surprise when, on the first day of camp, on my way to find some ice, someone shouted "Hello Taffy, I've just been reading about your Lightning flight!!" The world seemed a very small place. On returning to the U.K. I was overwhelmed to find that the incident was still front line news. People wanted to write articles in newspapers, books, magazines, interviews on TV and radio and underhand attempts to hear my account of what had happened. Having admitted that I had made an unwise decision to do the ground tests, I decided that the unwanted publicity that I had attracted was in no way going to be for financial gain. I steadfastly refused offers although for a two page article in the Sunday Express, I requested the editors to make a contribution to the R.A.F. Benevolent Fund. Despite prompts, no moneys were ever handed over and I became very disillusioned with all publicity media. Some friends thought I had gained reward for an article in 'Mayfair'; it was written without my knowledge and authority, but, because it was factually correct, I had no redress from the Press Complaints Board. Nonetheless, I was extremely annoyed.

    Some years after the incident, my hidden fears of high speed flight came to the surface and I had to spend two periods in hospital. I had not come to terms with the emotional side of the event. To return to my wife and family after five close encounters with death, was indeed a miraculous experience, but I had not been honest with myself, to accept it as such, so I needed psychiatric help. I could recall the technicalities of the flight without any hang-ups, but was unwilling to talk about that emotional side of the ordeal until I was placed under medical drugs and to bring those emotions to the surface. That was a rewarding experience and it gave me a much better understanding of people who might need that same kind of help, after similar unfortunate occurrences.

    Forty Years On

    I am now retired and living with my wife in Cheshire. Apart from being an active DIY plumber, carpenter, electrician handyman, my main pastime is involvement with family history. My inadvertent flight is still very vivid and in writing this personal account, I needed little prompting. Over the intervening years, I have received many letters and reminders from people whom I did not know, all praising my efforts to return myself and aircraft back to the ground safely. Yes, I have basked in some glory, when accounts of what happened, have been retold in social gatherings. I have never sought publicity, but whenever it became impossible to suppress, I have had to live with it. I enjoyed my career in the Royal Air Force, but not because of XM135!

    Best regards

    Taffy Holden
     
  13. James_Woods

    James_Woods F1 World Champ

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    I miss this thread - I think it may have been the best Aviation section thread of all time.
     
  14. Bob Parks

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    The original R3350's weren't just tempermental , the were just plain lousy engines. Cooling problems, oil loss( one of our crew chiefs claimed that it was the only externally oiled engine in the Air Force), internal metal failure (some engines failed after only 5 or 6 hours) , they put out the same horse pressure as an R2800 and had 1560 more cubic inches and higher specific fuel consumption.The configuration strongly hinted that that Curtiss Wrong built the engine with two R1820's face to face and I read where they were indicted during the war and after for knowingly signing off bad parts by bribing inspectors. Then the Curtiss Electric props were another source of constant failure. I watched a B-50 crash when the #3 and #4 CE props went into feather shortly after take off while still under full throttle. I have already mentioned the Curtiss SB2C as being a bad airplane with prop and engine problems plus many other things. Built to replace and surpass the SBD, it failed totally to meet it's objectives and the old Slow But Deadly had to soldier on.
     
  15. Gatorrari

    Gatorrari F1 World Champ
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    During the early '60s, I lived almost directly under the usual approach path to San Juan International Airport in P.R. This was about the point where pilots lowered flaps and landing gear, and they'd usually throttle up. When I heard a lot of popping and banging going on, I figured it was probably a Connie or a DC-7 (both R-3350 powered), and I was generally right. The planes with R-2800s, namely DC-6s and Caribair's Convairliners, were much less dramatic; the R-3350s sounded like they were about to fall off of the wing!

    No wonder the DC-6 outlasted the DC-7 in both passenger and cargo service. I would have liked to have seen the proposed turboprop DC-7D.
     
  16. Gatorrari

    Gatorrari F1 World Champ
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    #91 Gatorrari, May 31, 2013
    Last edited by a moderator: Sep 7, 2017

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